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wnt . 0 N Kcx 1 ' FF <br /> RIVERSIDE PUBLIC U'T'ILITIES <br /> _ J <br /> Boaxd Memorandxn <br /> PUBLIC UTILITIES <br /> BOARD OF PUBLIC UTILITIES DATE: April 15, 2011 <br /> ITEM NO: 4 <br /> SUBJECT: HUNTER SWITCHGEAR NO. 3 AND NO. 4 BUS TIE REPAIR —WORK ORDER NO. <br /> 1112682 <br /> ISSUE: <br /> Board of Public Utilities approval is requested for Work Order No. 1112682 and for the purchase of bus, bus <br /> supports, and bus duct for the Hunter Switchgear No. 3 and No. 4 Bus Tie Repair, <br /> RECOMMENDATIONS: <br /> That the Board of Public Utilities: <br /> 1. Approve Work Order No. 1112682 in the amount of$105,450 forthe Hunter Switchgear No. 3 and <br /> No. 4 Bus Tie Repair; and <br /> 2. Approve the purchase of bus, bus supports, and bus duct from Myers Power Products in Ontario, <br /> California, for the amount of$53,229 including sales tax. <br /> BACKGROUND: <br /> Hunter Substation is one of the City of Riverside's (City) 14 substations which distribute power to Riverside <br /> Public Utility(RPU)customers(see attached vicinity map). Hunter Substation has six main transformers that <br /> reduce the electrical voltage levels from 69 kilovolts (kV) to 12 kV or 4 W. Each of the six transformers <br /> feeds a corresponding lineup of switchgear including medium voltage bus work and circuit breakers. Each <br /> lineup of switchgear generally has a main bus tie, comprised of bus and bus duct, which allows a lineup of <br /> switchgear to be connected to another lineup of switchgear. This main bus tie is important because it allows <br /> RPU to maintain power to a lineup of switchgear when its corresponding transformer is taken out of service <br /> which provides operational flexibility in the event of equipment failure. <br /> In late December 2010,the main bus tie between Switchgear No. 3 and No. 4 at Hunter Substation failed on <br /> two occasions and resulted in customer outages. The first main bus tie failure occurred on December 23, <br /> 2010 when a section of the bus inside Switchgear No. 3 short circuited to ground. This caused Switchgear <br /> No. 4 to lose power for a number of hours, but customer power was quickly restored by circuit switching <br /> outside of the substation. Switchgear No.4 was put back into service after removing the section of damaged <br /> bus. On December 24, 2010, the second main bus tie failure occurred when a section of the bus duct short <br /> circuited to ground. This caused Switchgear No.4 to lose power again until the damaged section of bus duct <br /> was physically and electrically isolated from Switchgear No. 4. <br /> An investigation by staff revealed that the bus insulation failed for a number of reasons. First of all, moisture <br /> was a contributing factor as the humidity levels hovered at or below 100%during the time of the failure. Also, <br /> dust and particle infiltration was also a contributing factor to the failure. Furthermore, insulation abrasion due <br /> to the original bus support design was also suspect. Finally, natural degradation of the insulation was <br /> suspect because the bus and bus duct are more than 40 years old and have reached the end of their useful <br /> life. <br />